mitzy
- 07 Sep 2010 13:42
- 355 of 544
Missed that too..
Balerboy
- 07 Sep 2010 13:44
- 356 of 544
How about XEL spudding in progress?
robnickson
- 07 Sep 2010 19:55
- 357 of 544
Encore still has plenty of potential, not too late to get in , as does Xcite.
robnickson
- 08 Sep 2010 21:37
- 358 of 544
Should be an update by the end of this week , or maybe they will release the news in the weekend papers like last time.
robnickson
- 09 Sep 2010 17:06
- 359 of 544
Happy days !
Big Al
- 09 Sep 2010 18:11
- 360 of 544
This has done rather well, hasn't it? ;-)
robnickson
- 09 Sep 2010 18:36
- 361 of 544
Yes, in a short space of time also. Only bought into them a while ago after the Catcher find , at 52p.
required field
- 10 Sep 2010 10:25
- 362 of 544
Fantastic performance.....but hope it will not do a Bowleven ...that is profit taking on results......it might.....because a lot is in the sp now....
robnickson
- 10 Sep 2010 12:49
- 363 of 544
Guess it depends on how much recoverable oil they have found ? Plus takeover rumours always help .
gibby
- 10 Sep 2010 13:26
- 364 of 544
http://brokermandaniel.com/
required field
- 10 Sep 2010 16:38
- 365 of 544
Sold out and then had a change of heart right at close of play and bought back same amount....heck of a lot of pay to be tested...wondering if they have not discovered more than they think.....
robnickson
- 10 Sep 2010 17:08
- 366 of 544
I sold 10 percent of my shares at 94p today, too many times i have made paper profits only for them to fall back down again. Still lots to look forward too.
gibby
- 13 Sep 2010 07:48
- 367 of 544
robnick - nothing wrong banking profits - may want to buy back in today though? gl
Balerboy
- 13 Sep 2010 07:56
- 368 of 544
EnCore Oil plc (LSE: EO.) is pleased to announce the result of testing operations on the Cladhan appraisal well, located in UK Northern North Sea Block 210/29a.
The well, 210/29a-4Z flowed at a stable rate of circa 5,903 bopd (barrels of oil per day) for over 13 hours through a 28/64 inch choke with a final wellhead pressure of 1,874 psi (pounds per square inch). The flow rate was restricted by the capacity of surface facilities and due to the small diameter of the testing tools and the 3.5 inch tubing used while testing. The Operator, Sterling Resources, has indicated that with larger 4.5 inch completion tubing, they estimate that the well is capable of producing over 15,000 bopd. The testing confirmed light oil with a gravity of approximately 34 degrees API and a gas oil ratio (GOR) of 245 scf/bbl.
After completing the well test operations, the well will be plugged back and a further side-track downdip and to the southeast of the original discovery well will be drilled to better understand the location of the oil water contact (OWC) in the field. The side-track operation will commence later this week and is expected to take approximately two weeks subject to weather and operational delays.
cynic
- 13 Sep 2010 08:00
- 369 of 544
clunk for CEY but click for TLW and possibly for EO
required field
- 13 Sep 2010 09:52
- 370 of 544
Out again.....lot in the sp...and a month at least for next piece of decent news....
required field
- 13 Sep 2010 09:55
- 371 of 544
My mistake ..3 weeks.....so to be in or not to be in, that is the question ?....
Balerboy
- 13 Sep 2010 10:17
- 372 of 544
think you should be in and npe, sure there's more to come soon. edit, with xel still to perform.
Balerboy
- 17 Sep 2010 20:14
- 373 of 544
More news on drilling in about 10 days.....sp creeping up slowly